Installed the B&M Pro-Stick automatic shifter.
This works very well, and I like it much more than the ratcheting shifters. I also moved it back towards the seats, instead of being all the way up under the dash. Now the carpet needs to be redone to hide the giant hole. I have to call B&M because the neutral safety switch doesn't work appropriately.
The carpet is now cut so it "flaps" over the seats, so it looks much cleaner.
Locked the column shifter in place so that it does not swivel anymore.
Here I will write all about my progress on restoring my GTO. Read on to see what's going on.
Monday, August 3, 2009
Sunday, July 26, 2009
Monday, July 20, 2009
Last week, went to the Edison Light Cruisers show and my suspension dropped out on the left driver side. We did win a trophy though!
Sunday, installed the new heavy-duty springs and KYB shocks just to get her back on the road. The car rides MUCH higher (about 2 inches) and there are NO rubbing issues. Very excited for the change.

Sunday, installed the new heavy-duty springs and KYB shocks just to get her back on the road. The car rides MUCH higher (about 2 inches) and there are NO rubbing issues. Very excited for the change.
Sunday, May 24, 2009
Sound!
This weekend, we put in 4 pioneer speakers.
Front - Pioneer 6.5s in molded kickpanels
Rear - Pioneer 3-way 6x9s on the rear decklid (needed to cut and grind 2 holes to fit them).
Also removed REVERB box
Tested, and everything works well!

Rear decklid

Pass kickpanel

Driver kickpanel
Updated Engine bay pics



Next project: Paint parts of engine bay, replace Edelbrock carb with Holley carb, fix horns.
Sometime soon: Replace suspension.
Front - Pioneer 6.5s in molded kickpanels
Rear - Pioneer 3-way 6x9s on the rear decklid (needed to cut and grind 2 holes to fit them).
Also removed REVERB box
Tested, and everything works well!
Rear decklid
Pass kickpanel
Driver kickpanel
Updated Engine bay pics
Next project: Paint parts of engine bay, replace Edelbrock carb with Holley carb, fix horns.
Sometime soon: Replace suspension.
Sunday, May 17, 2009
Begin Car Season 2009
Friday, October 10, 2008
Saturday, September 27, 2008
Ignition switch
Replaced the ignition switch, took out the "start button". Now the key switch works correctly.
Monday, September 1, 2008
Friday, August 22, 2008
Distributor fix
There has been a lot of hesitation from idle, and the timing was way off, so we thought to put the dist back in at TDC and see if that took care of having the timing way off. Plus, I had a Pertronix ignitor II I wanted to install.
Everything was very easy to put together, and my dist was off by 1, but my timing is still waay off. This did make it easier to start and less hesitation than before. Idle is back down to about 900 rather than 1100 though.
Everything was very easy to put together, and my dist was off by 1, but my timing is still waay off. This did make it easier to start and less hesitation than before. Idle is back down to about 900 rather than 1100 though.
Friday, August 8, 2008
Finally after a year of waiting, the GTO is on the road. last week, we spend Thursday, Saturday and Sunday working on the disc brakes. Finished up everything, and the tires did not fit in the front. Monday, called up Firestone and ordered smaller front tires (215/65/15) - got them on Thursday, and they fit well. I rub on right turns, but right now I can't do anything about that. I have to install newer heavy-duty shocks to fix that.
Also changed the timing, it is WAY off, but the hesitation isn't so bad. I do stall if I don't give it enough gas from idle, but now I can floor it without a HUGE hesitation. Uncle Jim says the distributor may be off a tooth or 2.
I should make it to the Cranford Car show on Thursday, August 14th.
Also changed the timing, it is WAY off, but the hesitation isn't so bad. I do stall if I don't give it enough gas from idle, but now I can floor it without a HUGE hesitation. Uncle Jim says the distributor may be off a tooth or 2.
I should make it to the Cranford Car show on Thursday, August 14th.
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